by 59.46 million Baht or 17.25% as compared to Q1/2 018 following to the increasing sales volume due to household customer. The company has well controlled of the electricity cost, however raw water
purchasing raw water from private source. However, the company was able to save the electricity cost by 61.83 million Baht because the company has stopped transferring water from Nongplalai reservoir to
raw water from private source. However, the company was able to save the electricity cost by 56.60 million Baht because the company has stopped transferring water from Nongplalai reservoir to Chonburi
consolidated results. Fuel cost has been reduced significantly and would show full positive impact for the rest of the year. Electricity costs is expected to be reduced as we have started to generate electricity
investment picked up in line with the improved economic outlook, and with additional support from the government investment project even in this quarter its growth was lower than the assessment as the delayed
investment picked up in line with the improved economic outlook, and with additional support from the government investment project even in this quarter its growth was lower than the assessment as the delayed
due to flooding in the Alabama region which led to delayed receipt of its key raw material namely Mixed Xylene, thereby resulting in lower operating rate (26 days). Core EBITDA was $192 million (+35
impacted due to flooding in the Alabama region which led to delayed receipt of its key raw material namely Mixed Xylene, thereby resulting in lower operating rate (26 days). Core EBITDA was $192 million (+35
/2018. This was due to the deferred tax of Baht 70 million from closing ILM Malaysia, recognized in Q4/2018. Q4/2019 vs Q3/2019 (QoQ) 2019 vs 2018 (YoY) • Finance costs were Baht 45.5 million in Q4/2019
Xayaburi Hydroelectric Power Project, for a period of 31 years from the Commercial (Translation) 5 Operation Date, for sale of electricity as produced to the Electricity Generating Authority of Thailand